




May 24th, 2010. Seems I'm on a roll. After work today, I decided to change the linkage on the tranny to get it to shift with the right side of the shifter that indexes one gear at a time. That seems to have worked. Also, I changed the vacuum modulator by 2 turns inward to get a better shift between 1st and 2nd. That might also have helped. Lastly, I had already moved the rear pipes to get rid of the knocking noises when moving the tranny between reverse and drive. That did not work so something is hitting somewhere. Now, remember the loose header pipes? Seems one side has developed a leak so off to Kerns to get a gasket. I decided to section the area that was leaking so that worked but in the mean time, I saw where the 2nd pipe on the left was very close to the frame. AH HA!! The noise! I took the electric hack saw and removed a small part of the frame, along with part of a header pipe!!!!!!!. Oh my God! What did I do? Off to Dads to get the Mig welder. After welding, it seems OK but now there isn't any powder coating on that area. SH**! May 31st 2010. I have made a few adjustments to different things but will do a couple later. As of now, the car is as much done as possible, depending on if Joe re-paints the trunk and a couple touch-up spots. Today I copied the videos I made during the last 5 years unto a DVD. I saved that for last! I think this is my last entry to the blog so I hope you enjoy the last photos and the fruit of my labor.

















